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and Nishioka M., “ Supersonic Mixing and Combustion Control Using Streamwise Vortices,” AIAA Paper 1998-3271, 1998. and Hsu K., “ In-Stream Hypermixer Fueling Pylons in Supersonic Flow,” Journal of Propulsion and Power, Vol. 25, No. 4, 2009, pp. 885–901. P., “ Evaluation of Parallel Injector Configurations for Mach 2 Combustion,” Journal of Propulsion and Power, Vol. 8, No. 2, 1992, pp. 491–499. White F., Viscous Fluid Flow, 3rd ed., McGraw–Hill, New York, 2006, pp. 505–570. Unsteadiness within the flameholding region also varied greatly over the range of conditions studied, and largest unsteadiness was observed at intermediate boundary-layer heights.

It was found that flame shape changed, the persistence of the vortex cores was reduced, and combustion efficiency rose as the incident boundary layer grew. By varying the boundary-layer thickness from 40% of the ramp height to 150% of the ramp height, changes in the combustion flowfield downstream of the injector could be diagnosed. The experiment was equipped with a variable-length inlet duct that facilitated varying the boundary-layer development length for nearly constant injector shock structure conditions. Nominal test section entrance conditions were Mach 2, 131 kPa static pressure, and 756 K stagnation temperature. Goto, Florida Institute of TechnologyGraduate:"Vibration Control of Thin Plates with Periodically Distributed Shunted Arrays“ - F.The combustion field downstream of a 10 deg compression ramp injector has been studied experimentally using wall static pressure measurement, OH planar laser-induced fluorescence, and 2 kHz intensified video filtered at 320 nm for OH emission. Air Force AcademyUndergraduate Team:"The Design and Construction of a Blended Wing Body UAV“ – B. General Aviation Systems Award Kimbery Lemon, Wichita State University Open Topic Awards Ashley Korzun, Georgia Institute of Technology Chelsea Sabo, University of Cincinnati Carl Seubert, University of Colorado ChandrashekharTiwari, Pennsylvania State University Thanks Prof Randy Truman (UNM ) and Great Support from SAC and TCsĢ011 International Student Paper Competition Winners Undergraduate:"Experimental Aerodynamic Investigation of NASA Orion Forward Bay Modifications“ - TJ West and D. Student Activities – Membership Goal, 9000 by 2014Ģ010 Graduate Awards Zarem Award Aero – Michaels Isenberg, Cornell University Astro – Michael Jonell, Wright State University Orville & Wilbur Wright Award Joseph Galante, University of Maryland Brandon Jones, University of Colorado Julie Parish, Texas A&M University Adam Trebs, Purdue University John Leland Atwood Award David Wiese, University of Colorado William T.
